Experimental Physics and
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Hello all, I have been trying to develop a stepper motor control system using the Base release R3.15.2 and SynApps_5_8. I have followed the documentation in the motor record to setup the IOC for the MCB-4B controller board. Using the IO traces I can tell that communication with the board is happening (there is a constant polling of position and responses from the board, etc.), but whenever I try to change a value for a motion field I get the following:2017/02/08 10:53:40.203 devMotorAsyn::asynCallback: Enge:m1 pasyn{Float64,Int32}->write returned 2017/02/08 10:53:40.203 asynMotorController:writeInt32 error, status=3 axis=0, function=4, value=0 2017/02/08 10:53:40.203 devMotorAsyn::asynCallback: Enge:m1 pasyn{Float64,Int32}->write returned
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ANJ, 21 Dec 2017 |
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